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Re: (ET) ok, not the fusible link




Dammit! Ok, apparently it's NOT fixed. I was able to drive out to the yard. I was able to turn on the mower deck while sitting still. As soon as I then tried moving, with the deck on, the drive motor cut out. The blades kept moving until I turned the deck off - and of course won't start back up (the blades or anything else). Seems to be the same symptoms as I had before *after* replacing the blown fuse and soldering back together the fuse block. (the fuse didn't blow this time) When I engage the power disconnect and try driving, I hear a click, the power use gauge jumps up into the yellow, but nothing happens (no drive motor engaged). When I try engaging the PTO (mower deck), nothing happens (no power use change, no mower deck coming on). It seems like there's some short in the drive motor circuit somewhere. Just before it cut down, I engaged the blades, and the power use spiked to red as it started spinning the blades, then came down to the high end of the green (those gator blades seem to use a lot of power - I think I'll switch back to the regular ones). When I then tried driving, with the mower deck on, the power use gauge spiked red, and I moved about an inch before the drive motor cut out.
        I'll start looking through the drive motor line. Any ideas?

Thanks,
Mike



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Michael S. Briggs
UNH Physics Department
(603) 862-2828
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On Sun, 30 Jul 2006, Michael S Briggs wrote:


Ok, update on this - I seem to have it working now. I checked CB-1 this morning, and it was fine (although it may have tripped and had to cool down - how long does it normally take for CB-1 to cool down and close again?). Checked the power disconnect, and it's fine. I put a new inline fuse holder in where the control fuse goes on the fuse block, with a new fuse. I also checked the main power switch, and it's fine. So, being stumped about why it stopped working, I decided to just give her another try since I had replaced that bad fuse block terminal with a new inline fuse - and she works! I'll still go through again and do some more inspecting for melting insulation on wires, that could have caused the smoke, but as of now, it seems like the only problem was the blown control fuse, which then blew that part of the fuse block (so just replacing the fuse didn't get it working). CB-1 *may* have been tripped also though, I'm not sure.

Thanks for your help guys,
Mike